StreetStangs.net  

Go Back   StreetStangs.net > Technical > Ford Pushrod Tech (5.0 & 5.8)
FAQ Community Calendar Today's Posts Search

Reply
 
Thread Tools Display Modes
Old 12-29-2008, 02:58 PM   #31
militarymustang88gt
Senior Member
 
militarymustang88gt's Avatar
 
Join Date: Jun 2007
Location: bham and auburn
Posts: 337
i thought you were talking about the connector on the dis. that is your whole prob. if you look at the stock conector on the coil it has a whole bunch of plastic so it wont collapse the field. if it is just in the open it will colapse the magnetic field early and you may get 10,000 volts to the spark plug and look like you have spark but in reality you need 30,000 at least to run on these motors.



ps i suck on paint
__________________
finally got my avatar. it is the white one.
militarymustang88gt is offline   Reply With Quote
Old 12-29-2008, 03:01 PM   #32
StangChik
Senior Member
 
StangChik's Avatar
 
Join Date: Sep 2006
Posts: 194
good deal....I'll try that, because this is the first thing we noticed when it quit, but didn't think it was serious. Pull a part, here i come.
StangChik is offline   Reply With Quote
Old 12-29-2008, 03:02 PM   #33
waypastcrazy
ADDICTED TO SMALL BLOCKS
 
waypastcrazy's Avatar
 
Join Date: Jan 2007
Location: lookout mt
Posts: 1,757
pull number one plug bring #1 piston to top dead center of compression stroke pull dizzy cap and see where rotor button is sitting if its jump time it will be off from #1 terminal make sure 0 is lined with timing pointer on harmonic balancer if all is well check your vaccum line running to your map sensor. shot in the dark but had that happen on a friends bronco but it would crank just wouldnt stay running they worked on it for over a year.changed everything even the map.they finally gave up and came and got me and i lucked up and spotted the vac line had melted to back side of exhaust manifold. i am not familiar with your year model just figured i would throw something out there. good luck.
__________________
http://alabamaopencarry.com/forum/index.php
One of StreetStangs class clowns!
Status:slow as hell!
NORTH EAST ALABAMA STANGS
waypastcrazy is offline   Reply With Quote
Old 12-29-2008, 03:20 PM   #34
EHardy1971
Trunk Monkey
 
EHardy1971's Avatar
 
Join Date: Jun 2007
Location: Home
Posts: 5,708
Quote:
Originally Posted by StangChik View Post
its the connector on the coil not the dist. We have had 2 wires running to it, and they are brown and yellow i think.

What what worries me is the manual i have shows 3 wires.
Ok,on the coil,you should have 2 wires on the positive side,one is black that is supposed to go to the radio noise filter,the other is red/light green from the ignition switch. On the negative side it shows a dark green/yellow that goes to the ignition box. That brings up another possibility,being an '86,it has the duraspark ignition,and those things are notorious for going bad with no warning. If it has'nt jumped time,I'd take the duraspark box to the parts store to get it tested.
__________________
Eric
89 LX Coupe-Juiced
01 Lightning-Boost
06 TBSS
EHardy1971 is offline   Reply With Quote
Old 01-07-2009, 01:09 PM   #35
EHardy1971
Trunk Monkey
 
EHardy1971's Avatar
 
Join Date: Jun 2007
Location: Home
Posts: 5,708
Well,any luck?
__________________
Eric
89 LX Coupe-Juiced
01 Lightning-Boost
06 TBSS
EHardy1971 is offline   Reply With Quote
Old 01-07-2009, 01:10 PM   #36
StangChik
Senior Member
 
StangChik's Avatar
 
Join Date: Sep 2006
Posts: 194
haven't got back to it yet....haven't house trouble now
StangChik is offline   Reply With Quote
Reply


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -6. The time now is 09:20 AM.


Powered by vBulletin® Version 3.8.2
Copyright ©2000 - 2024, Jelsoft Enterprises Ltd.